|本期目录/Table of Contents|

[1]贺安新,赵福利,闵正红,等.超重力辅助强化油浆脱固技术[J].石化技术与应用,2022,3:186-189.
 HE An-xin,ZHAO Fu-li,MIN Zheng-hong,et al.Enhanced oil slurry solid removal technology under super-gravity assistance[J].Petrochemical technology & application,2022,3:186-189.
点击复制

超重力辅助强化油浆脱固技术(PDF)

《石化技术与应用》[ISSN:1009-0046/CN:62-1138/TQ]

期数:
2022年3期
页码:
186-189
栏目:
出版日期:
2022-05-10

文章信息/Info

Title:
Enhanced oil slurry solid removal technology under super-gravity assistance
文章编号:
1009-0045(2022)03-0186-04
作者:
贺安新1赵福利2闵正红1吴巍2王泽爱1
1.中海油惠州石化有限公司,广东 惠州 516086;2.中海油天津化工研究设计院有限公司,天津 300131
Author(s):
HE An-xin1ZHAO Fu-li2MIN Zheng-hong1WU Wei2WANG Ze-ai1
1.Huizhou Petrochemical Co Ltd, CNOOC,Huizhou 516086, China;   2. Tianjin Chemical Research and Design Institute Co Ltd, CNOOC,Tianjin 300131, China
关键词:
催化裂化油浆脱固传统沉降法超重力分离船用燃料油侧线试验
Keywords:
fluid catalytic cracking oil slurry removal traditional settling method super-gravity separation marine fuel oilside line test
分类号:
TE 624
DOI:
DOI:10.19909/j.cnki.ISSN1009-0045.2022.02.0108
文献标识码:
B
摘要:
利用超重力辅助强化技术和自主研发的TH-CJ型油浆沉降剂,在中海油惠州石化1.2 Mt/a 催化裂化装置中进行了催化裂化外甩油浆脱固侧线试验。结果表明:在实验室,采用传统沉降法需要48 h甚至更长时间才能将油浆灰分质量分数降至0.1%以下,如此可满足GB 17411—2015要求,而采用超重力分离技术侧线试验仅需要3 min;前者液体收率(质量分数)为85%~90%,而后者在97%以上;超重力分离侧线试验在连续稳定运行144个周期期间,油浆的脱灰率保持在86.21%之上,处理后油浆灰分质量分数始终低于0.1%,比传统沉降法更具技术优势。
Abstract:
By adopting the developed super-gravity assisted enhancing technology and the self-innovated TH-CJ type slurry settling agents, the sideline test of fluid catalytic cracking(FCC) external slurry solid removal was carried out in the 1.2 Mt/a FCC unit of Huizhou Petrochemical Co Ltd. The results showed that the traditional settling method in the laboratory required 48 h or even longer time to reduce ash content in slurry to less than 0.1% to meet the requirements specified in GB 17411—2015, while the sideline test that adopting super-gravity separation technology only required 3 min to meet the same specification mentioned above.The liquid yield of the former was 85%-90%, while that of the latter was above 97%. During 144 cycles of continuous operation in the supper-gravity separation sideline test, the solid removal rate had remained above 86.21%, and the mass fraction of slurry solid after treatment had been less than 0.1%. So this super-gravity separation technology had more technical advantages than the traditional settling method.

参考文献/References

[1] 董群,善世文,张国甲,等.催化裂化外甩油浆的净化与综合利用[J]. 化工进展,2010,12(Z 2): 28-32. [2] 杨玉祥.DCC油浆调和低硫船用燃料油的试验研究[J]. 炼油技术与工程,2021,51(11): 11-14. [3] 陈刚.催化裂化油浆综合利用浅析[J].广州化工,2016, 39(4): 38-40.[4] 陈卓, 肖宜春, 王伟. 炼厂催化裂化外甩油浆分离技术研究进展[J]. 化工技术与开发, 2016, 45(8): 27-29.[5] 杨杰. 助剂沉降法脱除催化裂化油浆中固体粉末的研究[D].上海: 华东理工大学, 2013.[6] 仲理科, 孙治谦, 任相军,等. 催化裂化油浆脱固方法研究进展 [J]. 石油化工, 2017, 46(9): 1209-1213.[7] 黄辉明, 杨成武, 马庆功,等. JR-SA 06高效油浆脱灰剂的工业应用[J]. 石油炼制与化工, 2019, 50(11): 21-25.[8] 贾中辉, 刘刚, 王旵东. XLT-C 80 A油浆沉降剂在大港石化公司的应用[J]. 石油石化绿色低碳, 2015, 5(6): 43-45.[9] 赵平, 蒋敏, 许世龙. 催化裂化油浆捕获沉降剂的工业应用[J]. 化工进展, 2015, 34(11): 4103-4107.[10] 黄占凯, 赵福利, 王会,等. 端氨基嵌段聚醚类油浆沉降剂的制备与表征[J]. 化工进展, 2021, 40(2): 755-762.[11] 曹炳铖.催化油浆净化技术及其化工利用的研究进展[J]. 石油化工, 2014, 41(3): 364-369. [12] 邹海魁, 邵磊, 陈建峰. 超重力技术进展——从实验室到工业化[J]. 化工学报, 2006, 57(8): 1810-1816.[13] 郭锴, 柳松年, 陈建峰,等. 超重力工程技术应用的新进展[J]. 化工进展, 1997,15(1): 1-4.[14] 郭爱军, 靳正正, 龚黎明,等. 助剂辅助催化裂化油浆离心-静电组合脱固工艺[J]. 化工进展, 2019, 38(7):3126-3135.[15] 王光卿. 稠油脱水效率影响因素的分析研究[J]. 中国石油和化工标准与质量, 2018, 38(7): 33-34.

备注/Memo

备注/Memo:
-
更新日期/Last Update: 2022-05-10