|本期目录/Table of Contents|

[1]谭都平,张峰,车春霞,等.碳二馏分加氢催化剂PEC-261的性能评价[J].石化技术与应用,2023,2:104-107.
 TAN Du-ping,ZHANG Feng,CHE Chun-xia,et al.Performance evaluation of PEC-261 catalyst for hydrogenation of C2 fraction[J].Petrochemical technology & application,2023,2:104-107.
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碳二馏分加氢催化剂PEC-261的性能评价(PDF)

《石化技术与应用》[ISSN:1009-0046/CN:62-1138/TQ]

期数:
2023年2期
页码:
104-107
栏目:
出版日期:
2023-03-10

文章信息/Info

Title:
Performance evaluation of PEC-261 catalyst for hydrogenation of C2 fraction
文章编号:
1009-0045(2023)02-0104-04
作者:
谭都平1张峰1车春霞1杨博1李保江2张生芳2彭远嘱2
(1.中国石油石油化工研究院 兰州化工研究中心,甘肃 兰州 730060;2.中国石油兰州石化公司 石油化工厂,甘肃 兰州 730060)
Author(s):
TAN Du-ping1ZHANG Feng1CHE Chun-xia1YANG Bo1LI Bao-jiang2ZHANG Sheng-fang2PENG Yuan-zhu2
(1. Lanzhou Petrochemical Research Center,Petrochemical Research Institute,PetroChina,Lanzhou 730060,China;2. Petrochemical Plant of Lanzhou Petrochemical Company,PetroChina,Lanzhou 730060,China)
关键词:
碳二加氢CO催化剂乙烯选择性乙炔性能评价
Keywords:
C2 hydrogenation CO catalyst ethylene selectivity acetylene performance evaluation
分类号:
TQ 426.95
DOI:
DOI:10.19909/j.cnki.ISSN1009-0045.2023.02.0104
文献标识码:
B
摘要:
对碳二后加氢催化剂PEC-261,根据单段和两段加氢工艺,在乙炔体积分数为0.60%~1.50%,体积空速为3 000 h-1的工况下,于工业侧线评价装置中进行长周期性能评价。结果表明:高体积分数CO物料的碳二加氢,其乙烯选择性最低为70%,明显高于常规单段碳二加氢的选择性(-20%);采用两段加氢,可达到较长运行周期和较高选择性的双重效果;单段加氢运行期间反应器出口乙炔体积分数低于2×10-6,乙烯总选择性达到90%以上,1 000 h长周期运行期间,反应器入口温度仅提高5 ℃,达到工业装置要求;在原料中有高体积分数CO时,PEC-261催化剂可以满足长周期运行的要求。
Abstract:
Under the condition with the acetylene volume fraction of 0.60%-1.50% and the space velocity of 3 000 h-1, the long-period performance evaluation based on the single-stage and two-stage hydrogenation process on the industrial siding evaluation device was carried out on PEC-261, a tail-end C2 hydrogenation catalyst. The results showed that during the C2 hydrogenation with high CO volume fraction, the lowest selectivity of ethylene was 70%, which was much higher than that of conventional single-stage C2 hydrogenation (-20%). The long operation period and high selectivity could be achieved by two-stage hydrogenation. During the operation of single-stage C2 hydrogenation, the volume fraction of acetylene at the outlet of the reactor was less than 2×10-6, and the overall selectivity of ethylene was more than 90%. During the 1 000 h long-period operation, the inlet temperature of the reactor increased only 5 ℃,which met the requirements of industrial plant. The PEC-261 catalyst could meet the requirements of long-term operation when there was high CO volume fraction in the feed stock.

参考文献/References

[1] 谭都平,温翯,沈立军,等.单段反应器碳二加氢催化剂工业侧线试验与工业运行[J].工业催化,2021,29(11):40-43.[2] 胡杰,王松汉.乙烯工艺与原料[M].北京:化学工业出版社,2018:636-669.[3] 侯维,谭都平,赵汝,等.影响两段直列式碳二反应器运行周期的因素[J].工业催化,2016,24(9):53-55.

备注/Memo

备注/Memo:
中国石油天然气股份有限公司资助项目(项目编号:LH-17-07-49-01)
更新日期/Last Update: 2023-03-10